Here's the deal. I finally got my GPX Moto 150 running in my CRF50 but now I'm trying to get it tuned right. It kicks over in 1-2 kicks and seems to idle decent, but if I let it idle for about 2-3 minutes the pipe starts to glow red. Does this mean that the Pilot jet is too small (lean)?
It seems to rev nice through 1/2 throttle but when I get passed that it stumbles and has very loud backfires on the deceleration. I've tried these main jets; 100, 110, 120, 130, and 150. I used the Keihin slotted round jets cause those are the only ones that work on this carb and out of all of them the 120 seem to work the best but you can still feel a power loss around 3/4 throttle and up and still loud ass backfires on decel.
I have not touched the pilot jet, so I'm leaning (no pun intended) towards putting in a bigger pilot jet to richen it up. From what I understand these 4 strokes like to run rich on the low end and lean on the top, does that sound right?
As far as the backfires are concerned I installed a gasket for the header at the head and tightened it down real nice and sprayed wd-40 around the intake and carb to check for air leaks and there was no fluctuation in the idle, so that leads me to believe that there isn't any air leaks. I'm assuming that it's backfiring because of the potential lean condition from the pilot jet. Can anybody confirm this?
Thanx in advance for the feedback!!!.....Manuel
It seems to rev nice through 1/2 throttle but when I get passed that it stumbles and has very loud backfires on the deceleration. I've tried these main jets; 100, 110, 120, 130, and 150. I used the Keihin slotted round jets cause those are the only ones that work on this carb and out of all of them the 120 seem to work the best but you can still feel a power loss around 3/4 throttle and up and still loud ass backfires on decel.
I have not touched the pilot jet, so I'm leaning (no pun intended) towards putting in a bigger pilot jet to richen it up. From what I understand these 4 strokes like to run rich on the low end and lean on the top, does that sound right?
As far as the backfires are concerned I installed a gasket for the header at the head and tightened it down real nice and sprayed wd-40 around the intake and carb to check for air leaks and there was no fluctuation in the idle, so that leads me to believe that there isn't any air leaks. I'm assuming that it's backfiring because of the potential lean condition from the pilot jet. Can anybody confirm this?
Thanx in advance for the feedback!!!.....Manuel